It was pretty wet but nothing major to worry about at that time because it was not dripping on the floor. The 2012 was the right time to take care of this issue during the restoration project.
First thing to do was the removal of steering gearbox. Well it was not easy even looking at the manual as a reference this procedure was hard as hell and impossible to do by one person, because there wasn't much space to maneuver.
ITR during steering gearbox removal.
The main crossmember without steering gearbox. |
Steering gearbox removed. |
Red marked seals have been replaced. |
Disassembled PS pump. |
PS pump after overhaul.
After putting everything back to working order I had to bleed the air from the system. This caused me headaches for a whole day because the pump was very noisy and I did notice bubbles in the reservoir (cavitational noise). The PS fluid I have used was the Honda genuine power steering fluid. I spent significant time running the engine and trying to get the air out of the system, but nothing worked. After many trials and errors I noticed that the system was sucking the air through the upper rubber hose attached to the pump. The hose did not have any clamp from factory. After the years it probably got hard and after putting everything back together it did not provide the necessary sealing. One simple metal clamp healed this issue, the air got out and the noise vanished immediately. I was relieved.
presne tak vyzera aj moje servo len s rozdielom ze som ho nezapchal izolackou ale dal som tam papier :)
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